Monday, May 11, 2009

Good read - Focus on Maintenance practices

Faulty maintenance blamed in MD engine fire
By: Paul Lowe


Two veteran American Airlines pilots, who in the words of the NTSB were “not having a good day,” nevertheless used “some exceptional stick-and-rudder skills” to get their crippled MD-82 safely back to Lambert-St. Louis International Airport (STL) after experiencing an in-flight engine fire during the airliner’s departure climb on Sept. 28, 2007.

During the return to STL, the nose landing gear on Flight 1400 failed to extend because of the loss of hydraulic pressure, so the pilots executed a single-engine go-around and lowered the nosegear using the emergency procedure. After the crew completed an emergency landing, the two pilots, three flight attendants and 138 passengers deplaned on the runway. No injuries were reported, but the airplane was substantially damaged by the fire.

The NTSB determined that the engine fire probably stemmed from an unapproved and improper procedure used by mechanics to start the left engine manually. The fire was prolonged and the safety of the MD-82 further jeopardized by how the crew handled the emergency, including a two-minute interruption to the engine-fire checklist.

According to the Safety Board, the use of an inappropriate manual engine-start procedure led to the uncommanded opening of the left engine air turbine starter valve and a subsequent left engine fire, which was prolonged by the flight crew’s interruption of an emergency checklist to perform nonessential tasks. Contributing to the accident were deficiencies in American’s Continuing Analysis and Surveillance System (CASS) program, the airline’s internal maintenance system.

The investigation revealed that a component in the manual start mechanism of the engine was damaged when a mechanic used an unapproved tool to initiate the start of the left engine while the aircraft was parked at the gate at STL. The deformed mechanism led to a sequence of events that resulted in the engine fire, to which the flight crew was alerted shortly after takeoff.

The Board examined how the flight crew handled the in-flight emergency and found their performance to be “lacking.” The captain did not adequately allocate the numerous tasks between himself and the first officer to deal effectively with the emergency.

The Board was particularly concerned about the fact that the crew repeatedly interrupted their completion of the emergency checklist items with lower-priority tasks, and this interruption–coupled with cascading systems failures–increased the pilots’ workload. The Safety Board also criticized the cockpit crew for a communications breakdown with the flight attendants.

NTSB acting chairman Mark Rosenker described the episode as an accident where things got complicated quickly and where flight crew performance was important. “Unfortunately,” he said, “the lack of adherence to procedures ultimately led to many of this crew’s in-flight challenges.”

Pre-existing Problem Not Solved

In examining the maintenance issues, investigators found that in the 13 days before the accident flight, the aircraft’s left engine air turbine starter valve had been replaced six times in an effort to address an ongoing problem with starting the engine using normal procedures. None of the valve replacements solved the engine start problem and American’s CASS did not discover the repeated failures to address the issue.

“The airline’s own internal maintenance system, the purpose of which is to catch maintenance and mechanical issues that could lead to an incident or accident, failed to do what it was designed to do,” said Rosenker. “And that allowed this sequence of events to get rolling, which ultimately resulted in the accident. Following the appropriate maintenance procedures would have gone a long way toward preventing this mishap.”

Although it deemed the captain’s decision to initiate a go-around to be “a reasonable choice,” the NTSB faulted the crew for the “lack of a sterile cockpit” while taxiing and for their response to the engine-fire warning light. Noting that while the pilots were “seasoned” and “professional,” Rosenker said, “What I heard on the CVR [cockpit voice recorder] seems to believe that.”

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Anonymous said............Some airlines to allow their pilots to take turns to nap. I don't see why the US shouldn't allow. I think being a pilot is a job that requires being constantly alert and fresh. I thought this video has got some interesting points about napping and how that can work out: www.newsy.com/videos/mid_air_mistake_sparks_debate_on_pilot_naps Oct 26, 2009 1137am.

Anonymous said...yes i think this is a good idea-(naps for pilots).

Anonymous said.......Is it possible in the near future we could get more MX Bases established for Mechanics? There is allot of Crews and Planes stationed in Knoxville,TN that would be an awesome place to work. I wonder if the company would even allow a temporary duty assignments say 30, 60 or 90 rotations? It certainly would give everyone a new incentive. Just a thought.

Anonymous said...CLT-we've been open down here for 4 1/2 years, is it too much to ask for a line shack? I've seen space come and go. peidmont has like 80 breakrooms and two trailers. Something? Maybe prevent a 10-15 min. trek each way? save fuel, delays. just a thought that has been going around for 4 years.July 16, 2009 9:16 AM

Greg Grant said... Thanks to everyone for the comments and analysis. Just a quick comment about the site. This is a blog dedicated to hearing from mechanic's and now aircrew all over Psa.
It is a place to get a little information and leave some. I get ideas and interests from everyone. I am not the only one giving input.
There are real MX issues at every station we know it we hear of it. The blog is a place to bring up those issues and discuss them with a healthy debate and hopefully come to a resolution.
If anyone has pics , video, articles or a Mx related issue. Send it in I will post your thoughts for all to read and respond to. Thanks again for the visit. Aug 8, 2009 1:15 pm

Karl Hanisch- Director of MX said...Good point regarding the engine training. You are correct that only about 1/3 of CLT has been to the line maintenance classes. I've asked training to secure slots in upcoming classes for CLT.

Joe Lindsey said...Regarding engine troubleshooting; For those not aware, the G.E. engine manuals contain T/S info for engine specific issues. Next time your CF34 acts up, don't just reach for the FIM and RACS alone...When you get to G.E. engine school, they cover in detail how to use the G.E. Manuals. Pay attention...it will come in handy.August 29, 2009 7:55 PM

Anonymous said.........usually management makes decisions based on bad or incomplete information from the mechanics themselves or MCC. Always make sure to give as much information as possible to MCC and confirm that they have it. There are some controllers who either do not take the time or do not know what to ask of the mechanics during the troubleshooting process. Make sure to keep them up-to-date. Sept 25, 2009

Anonymous said...I am fine with it. I've changed hundreds of tires with people boarding/deboarding. I always have at least one tire on the axle with the nut still installed if changing both wheel/tire assemblies...even if the aircraft is empty and in the hangar.July 18, 2009 6:34 PM

Anonymous said...so what does everyone think about the company wanting us to change tires with the aircraft on jacks as people are boarding?July 16, 2009 10:27 AM

Anonymous said...First, Clt would like to thank Kelley Perkey for coming down here to CLT to help out with N209PS #2 engine problem last week, thanks for your help. Acft N209PS was out of service for more than forty hours last week with an engine related problem. July 23 we here in CLT recieved a read and sign memo that we had to contact the Powerplant Manager whenever we have an engine related problem to help us with the troublshooting of these engine issues. We complied with the memo and he suggested to change the fuel control. He also convinced other people it was the fuel control. We would like to compliment the mechanics who worked on N209PS who knew it wasn't a fuel control and kept on troubleshooting this engine/air related issue. You all saved the company alot of time and money not changing the fuel control. Our thanks again to Kelley for helping out.August 15, 2009 8:17 AM